In the last post, I finally did some actual data logging with TinyCross set up in 4WD, 80A peak per motor, which is the rated current. Based on tinyKart, I know they can handle a a bit more for short durations, maybe even up to 120A. But the data logs (and many instances of having rocks flung into my face) demonstrate that the front wheels reach their traction limit somewhere around 60A on asphalt.
The behavior of front wheel slip on a go-kart is something new to me. In a straight line, the initiation of the slip and the acceleration of the wheel actually isn't the biggest problem. It's when the wheel regains traction and slows down that bad things happen. The restored grip combines with the energy being dumped from the wheel's moment of inertia to generate a quick pulse of torque on that side, which creates a lot of torque steer.
To deal with this, I wanted to implement some form of traction control, at least for the front wheels, so that I could get the most torque out of them as possible without the steering disturbances and rock shooting. But first, I needed a way to easily configure both the motor currents and the traction control settings without having to drag around my laptop everywhere. So, I finally built out the steering wheel UI to include a bunch of settings:
Sorry for the exposure; it's the only way to capture the full OLED refresh period. |
Anyone familiar with the MōVI Controller might recognize the OLED display. I chose this for daylight visibility and responsiveness (~50Hz update rate). The menu interface is essentially the same as the one I built the day before NAB 2014... The left knob scrolls through the menu. The right knob adjust settings and, by clicking or holding, performs actions.
In the four corners are three motor parameters for the corresponding motors: S for Status, which shows error codes. F for Forward peak current, and R for Reverse (braking, or actually reversing) peak current. Setting both to zero masks out the CAN command from that motor, triggering a timeout that turns off the gate drivers entirely. A click and hold on S triggers an encoder recalibration for that motor.
In the second column from the left, the first three settings relate to data logging: LS for Logger Status, FN for File Number (click to start a new file), and LT for Logger Time, the time in [ms] for a single row of the data log to be written. Then, there are two parameters for tuning traction control: TT for Traction Threshold, and TG for Traction Gain, which I will explain shortly.
The reason I wanted to be able to adjust peak currents from the steering wheel is because I agree with this early Tesla blog post: "...it's much safer to avoid wheelspin altogether than react to it." If I know the surface supports front wheel current around 60A, there's not much point in setting it higher than that. But, I want to be able to set it higher for testing, or adjust it for different surfaces.
As for the traction control itself, there are a lot of corner cases to think about in 4WD, but the main problem I'm trying to solve is front wheel slip. If I assume the rear wheels are not slipping, then I can use their average speed as a reference. From there, it's easy to see if a front wheels is running faster than that reference, and reduce the current to that motor if so. This only needs two settings: a Traction Threshold (TT) that sets how much wheel slip is allowed, and a Traction Gain (TG) that sets how much to reduce the current per unit slip above the threshold. The Traction Threshold prevents overactuation in normal conditions and allows for speed differential due to turning radius.
But what happens if a rear wheel does slip? Well, then the front wheel might slip too. At that point, I'm probably in some kind of a four wheel sideways drift anyway, so alternate control laws are going to apply. Being able to trigger some rear wheel slip with the throttle is part of the fun, too, so having complete 4WD traction control isn't something I necessarily need to solve.
With the new UI setup and the simple front wheel traction control in place, it was time to do some tuning...
...or not. |
At first, everything seemed to be going okay. I did a couple of runs at 60A front current and 80A rear current and the traction control seemed to be working as intended. But then during light regenerative braking at around 30mph, I heard the all-too-familiar sound of a FET popping, followed by some more bad noises and smells from the front drive. Upon inspection, only two FETs actually died, but they also took out many of the power traces, meaning this board was trash.
So what happened? Well, unfortunately, the data log was not very helpful in this case. It did show the speed (30mph) and current command (around -10A), but nothing out of the ordinary up until the point of failure. There is only one data point showing a Q-Axis current of 286A on the front left motor, followed by an undervoltage fault, which might have been the battery sagging or the power input traces getting blown up. So whatever happened, happened quick.
It's been a while since I've actually destroyed a motor controller, so I was a little disappointed. But after some thought, I didn't think this was due to the new traction control stuff. That's only applied during acceleration, and this failure definitely happened under braking. I think it's more likely that the front left motor just lost sync and the back EMF at 30mph was high enough to do damage. Up until now, I have only had a relatively slow overcurrent limit of 160A (or more) for 10ms. These FETs have a pretty insane Safe Operating Area (SOA), but that limit does leave room for exceeding it with currents above 400A:
This system could easily generate a 400A transient if a motor loses sync at 30mph. And the motor position and speed data does cut out at the same data point as the failure. But that's not enough to determine cause and effect. So for now I can only make changes that might help and hope for the best. I added in several more stages of faster overcurrent protection, up to 300A for a single ADC/PWM cycle (42.7μs). These overlap enough to cover the entire R_DS(on)-limited boundary of the SOA (up to the pulse rating of 1450A for 100μs!).
A faster overcurrent trip doesn't help with whatever caused the motor to lose sync in the first place (if that is what happened). I have seen at least a couple previous instances where the encoders, which supply emulated Hall effect sensor signals, have behaved as if they were completely reset. Even though I only use the buffered and optically isolated virtual Hall effect sensor signals for commutation, I was still reading the SPI data anyway. Maybe a SPI read got corrupted by noise and turned into a write that either reconfigured or entirely reset the encoder mid-run? To protect against this, I now disabled the SPI transactions entirely other than during initialization and calibration.
So with these changes and my last and only spare drive, I went back out for another try. This time, I ran into no motor drive issues and was actually able to test and tune the front wheel traction control as I originally intended. The difference is immediately obvious while driving and in the data. First, a test at 80A front, 90A rear, with no traction control:
Front wheel traction control off. |
As before, the front right wheel starts slipping at about 60A and spins up to 2-3x the actual ground speed. The front right always seems to lose grip first, a mystery to solve another day. When I let off the throttle and it regains traction, the torque pulse creates substantial torque steer, jerking the steering wheel almost 20º to the left, which I then have to counteract immediately to stay on course. Overall, it's impossible to sustain peak acceleration for more than a second or so before having to deal with the wheel spin and torque steer.
And now with the same currents, but front wheel traction control on:
Front wheel traction control on. |
The front right (FR) current now averages a bit below 60A and its speed is held to just a small margin above the actual ground speed. It's never able to build up momentum and then "catch", inducing torque steer. This allows continuous acceleration up to and past 30mph. The front left (FL) also starts to slip in the 20-30mph range, but the traction control catches it too. The overall result is a much more controllable launch and far fewer rocks being thrown up by the front wheels.
After finding traction control settings that I liked, I switched back to current settings that more closely match the actual traction limits: 60A front and 100A rear. This still gives a reasonable 0.45g launch, but with less likelihood of triggering the traction control on asphalt. I'd like to push to >0.5g, to match tinyKart's most extreme configuration, but that'll either require 120A on the rear or changing the gear ratio a bit. At 60A / 100A, the front motors still share enough of the load that the rear motors stay at healthy temperature after some acceleration runs:
Rear motors are doing most of the work, but... |
...they are at a reasonable temperature. |
And finally I did some less structured testing by just driving through the gravel corner in my parking lot and intentionally adding throttle to induce slip. It behaves pretty well, slipping and oversteering about the right amount to be controllable but still fun:
Mystery data log. |
Have you corner balanced the kart? That could be causing the FR to lose traction first. As always, fascinating stuff!
ReplyDeleteGood point - my first thought was a motor drive timing issue but I should check the corner balance first. Time to find four tiny scales.
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